Just received a new set of power supply, controller and stepper shield and everything looks correct as regards the port settings, etc. UGCS reports that it has connected to the port, but I don’t get the OK I’m used to seeing about a second after clicking Open. $X reports “No supported kill alarm clock for this version” and $H result in similar messages. Any attempt to move an axis results in the report “GRBL not finished booting.”
I’ve read the similar forum threads, and tried all things suggested as well as what I had to do to get the original controller to work. I even removed the Uno and shield from the enclosure to ensure no problems with the boards seating properly. But still have the problem.
Any suggestions from the community would be very appreciated. Thanks in advance.
Going through the forum for this issue shows it has been fixed by using the correct baud rate (115200) or reflashing the Arduino. Can’t think of anything else.